• Title of article

    Experimental study on combustion and NOx emissions for a down-fired supercritical boiler with multiple-injection multiple-staging technology without overfire air

  • Author/Authors

    Kuang، نويسنده , , Min and Li، نويسنده , , Zhengqi and Liu، نويسنده , , Chunlong and Zhu، نويسنده , , Qunyi، نويسنده ,

  • Issue Information
    روزنامه با شماره پیاپی سال 2013
  • Pages
    8
  • From page
    254
  • To page
    261
  • Abstract
    A deep-air-staging combustion technology was previously developed to achieve reduction in NOx emissions and to eliminate strongly asymmetric combustion found in down-fired boilers. Recently, one of two down-fired 600 MWe supercritical utility boilers using this technology (without applying overfire air) began commercial operations. To understand coal combustion and NOx emissions characteristics within the furnace, full-load industrial-size experiments were performed at different air-staging conditions with measurements taken of gas temperatures in the burner region, gas temperatures and species concentrations in the near wing-wall region, carbon content in fly ash, and NOx emissions. As expected, the furnace performance characterized by relatively timely coal ignition, symmetric combustion, and low levels of carbon in fly ash, developed in the furnace at all three settings. Deepening the air-staging conditions could reduce NOx emissions by one-fifth, but varied slightly carbon in fly ash. In view of the still high NOx production (i.e., 1036 mg/m3 at 6% O2), adding an overfire air system which was essentially a part of the technology, was recommended for the boiler to significantly reduce the present NOx emissions.
  • Keywords
    Down-fired boiler , Coal combustion , NOx emissions , Industrial-size measurement , Multiple injection and multiple staging
  • Journal title
    Applied Energy
  • Serial Year
    2013
  • Journal title
    Applied Energy
  • Record number

    1606222