Title of article
Investigation of a concrete railway sleeper failed by ice expansion
Author/Authors
Zi، نويسنده , , Goangseup and Moon، نويسنده , , Do Young and Lee، نويسنده , , Seung-Jung and Jang، نويسنده , , Seung Yup and Yang، نويسنده , , Sin Chu and Kim، نويسنده , , Soo-Sam Kim، نويسنده ,
Issue Information
روزنامه با شماره پیاپی سال 2012
Pages
13
From page
151
To page
163
Abstract
We investigated a conical crack formed near a fastening bolt of a concrete railway sleeper in a slab track system. The crack initiated from the bottom of the sleeper and penetrated the sleeper completely forming a conical shape. To study the reason for this and to examine the failure mechanism, we used a three dimensional finite element method and a series of experimental programs. The result of the numerical simulation was verified with the experimental data. From this study, we concluded that the conical crack was caused by the volume expansion of the freezing water leaking into the plastic insert of the fastener hole. The effect of location of the frozen insert holes, initial fastening force and compressive strength of concrete on the freezing force was also studied in this study.
Keywords
fracture , Ice expansion , Finite element model , Slab track , Concrete railway sleeper
Journal title
Engineering Failure Analysis
Serial Year
2012
Journal title
Engineering Failure Analysis
Record number
2339582
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