Title of article :
Fatigue fracture of an AMX aircraft main wheel
Author/Authors :
L. and Amura، نويسنده , , M. and Allegrucci، نويسنده , , L. and De Paolis، نويسنده , , F. and Bernabei، نويسنده , , M.، نويسنده ,
Issue Information :
روزنامه با شماره پیاپی سال 2013
Pages :
9
From page :
194
To page :
202
Abstract :
A forged 2014-T6 aluminium alloy main wheel of an AMX aircraft failed during pre-flight taxiing. e occurred on the wheel housing hub and its origin was located on the interior edge of the bearing cup housing. The wheel experienced high cycles fatigue. A plastic deformation was produced during the wheel mounting operations caused an abnormal stress concentration. It has been identified as cause of a progressive fracture mechanism. Consistent optical, metallographic and electron microscopy evidences were collected. Moreover, Finite Element Analysis (FEA) demonstrated that the observed defects produced the stress level needed to fatigue to initiate. Recommendations were issued in order to improve the Non-Destructive Techniques (NDT) used to monitor the wheel structural integrity. Laboratory tests showed that ultrasounds in this case would be far more efficient than the prescribed eddy currents.
Keywords :
Aluminium alloy , Main wheel , ultrasonic , Fatigue failure , Eddy currents
Journal title :
Engineering Failure Analysis
Serial Year :
2013
Journal title :
Engineering Failure Analysis
Record number :
2339623
Link To Document :
بازگشت