Title of article :
Failure analysis of an aircraft nose landing gear piston rod end
Author/Authors :
Asi، نويسنده , , Osman and Ye?il، نويسنده , , ?nder، نويسنده ,
Issue Information :
روزنامه با شماره پیاپی سال 2013
Pages :
9
From page :
283
To page :
291
Abstract :
A failure investigation has been conducted on a piston rod end used in a hydraulic actuating cylinder of an aircraft landing gear. The failed piston rod end was found to be broken. An evaluation of the failed piston rod end was undertaken to assess its integrity that included a visual examination, photo documentation, chemical analysis, hardness measurement, tensile testing, and metallographic examination. The failure zones were examined with the help of a scanning electron microscope (SEM) equipped with EDX facility. A stress analysis is also carried out by the finite element technique for the determination of highly stressed regions on the piston rod end. The results indicated that the piston rod end failed by fatigue with cracks initiated at the surface close to the mechanically damaged region due to high stress concentrations.
Keywords :
Aircraft failures , Landing gear , Fatigue , Stress concentrations , Piston rod end
Journal title :
Engineering Failure Analysis
Serial Year :
2013
Journal title :
Engineering Failure Analysis
Record number :
2339765
Link To Document :
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