Title of article :
Fatigue energy dissipation and failure analysis of angle shear connectors embedded in high strength concrete
Author/Authors :
Shariati، نويسنده , , Mahdi and Shariati، نويسنده , , Ali and Ramli Sulong، نويسنده , , N.H. and Suhatril، نويسنده , , Meldi and Arabnejad Khanouki، نويسنده , , M.M.، نويسنده ,
Issue Information :
روزنامه با شماره پیاپی سال 2014
Pages :
11
From page :
124
To page :
134
Abstract :
To inspect the fatigue energy dissipation of angle shear connectors under fully reversed cyclic fatigue loading while embedded in a high strength concrete (HSC) slab, a series of experimental push-out tests was conducted. The experimental tests comprised eight push-out test specimens with different geometries of angle connector. The failure of the angle connector under monotonic and low cyclic fatigue loading was tested and the observations were discussed. The results show that the ductility performance for angle shear connectors embedded in HSC was inadequate. However, reasonable strength resistance under monotonic loading and a small amount of fatigue energy dissipation under cyclic fatigue loading for connector was detected. All push-out test specimens experienced connector fracture failure with very low energy dissipation when subjected to fatigue loading. Details of the failure analysis and fatigue energy dissipation of the angles in HSC are fully described in the results.
Keywords :
Angle Shear connector , push-out test , Fatigue loading , Failure analysis , Energy dissipation
Journal title :
Engineering Failure Analysis
Serial Year :
2014
Journal title :
Engineering Failure Analysis
Record number :
2340106
Link To Document :
بازگشت