Author/Authors :
Nakajima، نويسنده , , T.، نويسنده , , Suzuki، نويسنده , , K.-I.، نويسنده , , Yajima، نويسنده , , M.، نويسنده , , Kawakami، نويسنده , , N.، نويسنده , , Tanomura، نويسنده , , K.-I.، نويسنده , , Irokawa، Katsumi نويسنده , , S.، نويسنده ,
Abstract :
A dc component contained in a output of a
voltage source self-commutated converter makes a converter
transformer to be dc-magnetized, in the worst
case causing an overcurrent due to saturation. We experienced
the dc-magnetization of the converter transformer
of a 50 MVA self-conmutated SVC installed in the
Shinshinano Substation of Tokyo Electric Power Company
when system disturbances occurred by energizing of an
adjacent large capacity transformer.
After analyzing the problem, a novel dc magnetization
preventing control was developed that makes a fast
flux correction according to the voltage dc component
detected in the converter output. This method was applied
to the 50 MVA self-commutated SVC and produced
satisfactory operation results.
Keywords :
Self-commutated converter , GTO , DC magnetization , static var compensator , Voltage source converter