DocumentCode
1915154
Title
Failure analysis of 127mm G105 drill pipe
Author
Fangpo, Li ; Yonggang, Liu ; Caihong, Lu
Author_Institution
CNPC Tubular Goods Res. Inst., Xi´´an, China
Volume
2
fYear
2011
fDate
20-22 May 2011
Firstpage
1813
Lastpage
1816
Abstract
One Φ127mm G105 drill pipe body washed out infrequently just after 126h of pure drilling time. This paper gives a systematic analysis in consideration of both material quality and loading condition on drill strings. Measurement and inspection were performed on configuration, chemical compositeon, mechanical performance, metallograghy and micro-fractograghy. It´s thought that the drill pipe failure accident was premature fatigue failure accident. Failure reason is the 0.35mm decarburization layer caused by improper heat treatment and mechanical damage because of improper operating on the out surface. Under the effect of fluctuating stress, fatigue cracks originated from decarburization layer and grew rapidly. When cracks propagated through the wall thickness, drill pipe washed out.
Keywords
drilling machines; failure (mechanical); failure analysis; fatigue cracks; fractography; heat treatment; metallography; pipes; G105 drill pipe; chemical composition; decarburization layer; drill pipe failure accident; drill string; failure analysis; fatigue crack; fluctuating stress; heat treatment; inspection; loading condition; material quality; mechanical damage; mechanical performance; metallograghy; microfractograghy; premature fatigue failure accident; time 126 h; Artificial intelligence; Chemical elements; Chemicals; Iron; Pumps; Silicon; Surface cracks; decarburization layer; drill pipe; failure analysis; fatigue;
fLanguage
English
Publisher
ieee
Conference_Titel
Materials for Renewable Energy & Environment (ICMREE), 2011 International Conference on
Conference_Location
Shanghai
Print_ISBN
978-1-61284-749-8
Type
conf
DOI
10.1109/ICMREE.2011.5930687
Filename
5930687
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