DocumentCode :
2896581
Title :
Study on a real case of low frequency oscillation occurred in the black-start by a hydropower plant
Author :
Yang, Bo ; Jiang, Jing ; Yu, Tao ; Jiang, Jinliang
Author_Institution :
Dept. of Electr. Power, South China Univ. of Technol., Guangzhou, China
fYear :
2011
fDate :
6-9 July 2011
Firstpage :
1445
Lastpage :
1448
Abstract :
This paper recaptures a low frequency oscillation occurred during simulation and finally being resolved in the real grid. Three hypothesis are proposed to tackle this issue, namely the ferro-resonance caused by hasty stepping up, the inrush current derived from remanence in transformer and the parameter resonance between the unit and experiment grid. After being refuted consecutively it is assumed that the auto-excitation system parameter resonates with grid. Expectedly the oscillation vanished by altering the control parameter with proof of some simulation results. At last two conclusions are presented from experimental analysis.
Keywords :
ferroresonance; hydroelectric power; power system stability; black-start; ferroresonance; hydropower plant; low frequency oscillation; parameter resonance; Circuit faults; Hydroelectric power generation; Oscillators; Substations; Surges; Transient analysis; black-start; excitation system; low frequency oscillation; parameter resonance; stepping up from zero;
fLanguage :
English
Publisher :
ieee
Conference_Titel :
Electric Utility Deregulation and Restructuring and Power Technologies (DRPT), 2011 4th International Conference on
Conference_Location :
Weihai, Shandong
Print_ISBN :
978-1-4577-0364-5
Type :
conf
DOI :
10.1109/DRPT.2011.5994123
Filename :
5994123
Link To Document :
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