DocumentCode :
3581029
Title :
Optimization of the peak-load condenser operation for a fossil-fired generation unit with ACC
Author :
Haisheng Yang ; Shengyang Lu
Author_Institution :
Thermal Dept., Hebei Electr. Power Res. Inst., Shijiazhuang, China
fYear :
2014
Firstpage :
1
Lastpage :
4
Abstract :
For improving the economic benefit of the generation unit with ACC (air-cooled condenser) in summer season, a peak-load condenser system was updated for the ACC system. Optimization of the peak-load condenser operation was studied using the site test and system simulation methods. Based on the site test data, certain characteristic performance parameter was calculated such as cleaniness factor and etc. Final optimized operation scheme was studied using the simulation software for various ambient conditions. It is shown that, based on the current equipment conditions, for most of the weather conditions except for winter, the peak-load condenser with one cooling pump in operation can improve the unit performance.
Keywords :
condensers (steam plant); optimisation; pumps; steam power stations; ACC system; air-cooled condenser; cooling pump; fossil-fired generation unit; peak-load condenser operation optimization; site test method; system simulation method; Adaptation models; Cooling; Data models; Load modeling; Meteorology; Optimization; Poles and towers; ACC (air-cooled condenser); Fossil-fired Generation Unit; Optimization; Peak-load Condenser;
fLanguage :
English
Publisher :
ieee
Conference_Titel :
Power and Energy Engineering Conference (APPEEC), 2014 IEEE PES Asia-Pacific
Type :
conf
DOI :
10.1109/APPEEC.2014.7066045
Filename :
7066045
Link To Document :
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